| Video Clip | Event/Process Description | Outcome achieved via 20/20 Hindsight High Speed video Application |
 | Cans passing through a bubble breaker at 1800/minute. | Increased Uptime |
 | Seamer problem causes cans to be crushed. | Improved Product Quality |
 | Plastic bottles being filled with a sports drink. | Increased Equipment Uptime |
 | Can Jam. | Costly Downtime Reduced |
 | Filler Jam. | Efficiency Improvements Achieved |
 | Juice Box Filling. | Reduced Machine Setup Time |
 | Beer bottle reject process causing high quality to be rejected. | Improved Equipment Reliability |
 | Beer can seamer jams. | Improved Machine Reliability |
 | Partition glue gun inserter for beer bottles. | Reduced Production Cycle Time |
 | Bottles with inconsistent fill heights result in off-quality products. | Reduced Operating Costs |
 | Arm transfering PET to the blow molder. | Increased Uptime |
 | Glue Shot. | Increased Line Efficiency |
 | Doses of liquid nitrogen being applied to bottled water to improve stackability of the cases. | Reduced Costs |
 | Bottle capping on a PET bottling line. | Reduced Downtime |
 | PET bottles on a beverage line. | Improved Factory Throughput. |
 | Beer bottle falls off of a bottling line. | Reduced Lost Production |
 | Can of beer with a warped lid. | Ensured Proper Setup of Seamer Machine |
 | Problem with seamer machine causes cans to be crushed. | Reduced Scrap Costs |
 | Heineken 6-Pack Insert. | Increased Uptime |
 | PET Bottle Labeler. | Increased Line Speed and Efficiency |
 | Sport Drink Conveyor. | Increased Uptime |
 | Minor Capping Issues | Determined Line Fault |
 | Bottled water line – cocked cap issue | Ensured Line Integrity |